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Flight set 360T004 (STS-30)The performance of 360T004, Forth Flight, Redesigned Solid Rocket Motors (RSRM) is assessed in respect to joint sealing issues as seen from post-test inspection of the seals and sealing surfaces. The factory joint disassembly inspections for this flight set were omitted. The decision was based on the rational that there is sufficient information in the present data base, and this would give H-7 refurbishment operations faster turn around time for this set of hardware. The factory joint disassembly inspections will resume for 360H005, Fifth Flight, through 360L007, Seventh Flight, due to a new grease application being in effect during the assembly process. The left hand nozzle was forced into the snubbed position upon splash down. This required unique tooling to be manufactured to perform the disassembly of the internal nozzle joints. This was completed on February 5 and 6, 1990 at the H-5 Clearfield, Utah facility. The RSRM consisting of capture feature, field joints with the J-joint insulation configuration is illustrated. The nozzle-to-case joint design, which includes 100, 7/8-inch radial bolts in conjunction with a wiper O-ring and modified insulation design is also illustrated, as is the ignition system seals and a cross section of the igniter. The configuration of all internal nozzle joints is shown.
Document ID
19900012733
Acquisition Source
Legacy CDMS
Document Type
Contractor Report (CR)
Authors
Nelsen, Lowell V.
(Thiokol Corp. Brigham City, UT, United States)
Date Acquired
September 6, 2013
Publication Date
March 1, 1990
Subject Category
Mechanical Engineering
Report/Patent Number
TWR-17543-VOL-4
NASA-CR-183927
NAS 1.26:183927
Accession Number
90N22049
Funding Number(s)
CONTRACT_GRANT: NAS8-30490
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.
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